[关键词]
[摘要]
针对现阶段热电联产机组供热期调峰能力不足的问题,以某350 MW超临界燃煤机组为案例,介绍了其高低压旁路供热改造方案,并以改造后机组的实际运行数据为基础,对改造前后机组的运行特性和调峰能力进行了详细的对比分析。结果表明:案例机组进行高低压旁路供热改造后,在保证机组供热期热负荷和热段再热蒸汽流速不超限的情况下,机组电负荷调峰下限可由原来的230.9 MW降至161.4 MW,降低30.1%;当案例机组两个中压调节汽门关至42%时,机组电负荷调峰下限可进一步降至140.8 MW;旁路供热蒸汽量占比可由原来的56.3%提高至61.9%,提高5.6%,机组的调峰能力得到进一步提高
[Key word]
[Abstract]
In view of the problem of insufficient peak shaving capacity during the heating period of the cogeneration unit at current stage, the reformation scheme of HPLP bypass system combining with heating in a 350 MW supercritical coalfired unit was introduced. Based on the actual operation data of the unit after the reformation, a detailed comparative analysis of the operating characteristics and peak shaving capabilities of the unit before and after the reformation was carried out. The results show that after the HPLP bypass heat supply reformation, the lower limit of the unit′s electrical load peak regulation can be reduced from 230.9 MW to 161.4 MW with a reduction of 30.1%, by ensuring the heat load of the unit during the heating period is satisfied and the flow rate of reheated steam in hot section do not exceed the limit; when the two middle pressure regulating valves of the case unit are closed to 42%, the lower limit of the unit′s electrical load peak regulation can be further reduced to 140.8 MW; the proportion of bypass heating steam increases from 56.3% to 61.9% with an increase of 5.6%. The peak shaving capacity of the unit has been further improved.
[中图分类号]
TK262
[基金项目]
华北电力科学研究院青年创新项目(KJZ2022004)